Hi,
Lately I've been working with a direct heating controller to dump power from a wind turbine directly into a resistor bank. This controller is being built for a 240V 3kW exmork wind machine. The principle behing the controller is to use a RPM / power table to control the pulse width going to the load resistor.
The wind machine was coupled to an 11kW induction motor, which is being driven by a VFD. This setup was first used to gather voltage / speed / frequency data, since the information did not seem to be easily available. The generator is 8 pole, and unloaded AC voltage between phases is pretty much spot on 1V / rpm. Currently the setup is being used to load test the controller. Water heating elements visible in the background are used for testing.
(Larger version of drawing;
http://pics.ww.com/v/Janne/Electronics/P1060168.JPG.html)
Here's the functional blocks of the controller. First off, the 3-phase AC is rectified, and filtered to a pair of capacitors. The DC voltage is then chopped with the FET, L1 is used to smoothen the current / voltage transition speed. Switching frequency is 20kHz. The load resistor is sized so, that with full duty it should load the turbine more than sufficiently at rated speed. Assuming of course, that my calculations with efficiency etc. hold water
A picaxe microcontroller is used for determinig the duty cycle of the resistor. The power for the micro is derived directly from the main DC-bank, with the help of a 200VDC linear regulator + a swithed mode PSU that will accept DC input voltage. Speed input is derived from the generator's AC frequency, with the help of an optocoupler. The pulse width for the PWM generator is then loaded from a lookup table, which has been pre-calculated with an excel spreadsheet. The control part is pretty much the same as in my MPPT controller(which for some reason is still yet to be installed. Summer is clearly too short
). Diary about that can be found here;
http://fieldlines.com/board/index.php/topic,130334.0.html The controller itself. If it's home built, it's supposed to look like it, right?
. The cover also has an LCD display to show rotor rpm duty cycle, and mode of operation. The switch selects between manual and automatic control, automatic mode works with the lookup table and manual mode just takes input from the potentiometer also located in the cover.
So far the controller is working ok in the test bench with a few problems. The inductor needs to of larger physical size, it's getting too hot in operation. I only added it afterwards from my leftover parts bin, initially I tried to get away without any filter inductor, which was a bad idea to start with. The electrical interference was horrible. Same story with the diode, now with the added inductor the diode also gets to do some work = the small UF4007 diode is getting overwhelmed. The isolation between low and high voltage sides is also not proper, so that needs to be fixed too if a nicer version of the unit is built.
Then of course there is the fun of live testing it. There is no telling how (if) the furling on the machine will work, when it's being loaded with a better power curve, than originally intended. Propably it will need some tuning too. As a backup for the controller, we're also going to install a voltage tripped backup load, just in case the magic smoke escapes from the thingy. Some form of mechanical latch, details about that are yet to be figured out.