Hi all, first post here but I have been creeping around these forums for a few years now.
Thought I would share my current project of building a direct drive wind turbine air compressor. To get the initial efficiency comments out of the way... Yes, compressed air is the actual form of energy I need stored so this seems to be the best route with my location.
Bit of background: I live in a town where the average wind speed is South West 16-22kts from May till September. Spring and Autumn are neutral and then the wind switches to North East for the winter thou less consistent than the Summer. The Summer inflow begins around 11am, ramps up till 3:30pm, holds for a few hours and then backs off at 7pm. This incredibly predictable wind attracted Windsurfers in the 80's and 90's and then Kiteboarders in 2001 and on. The popularity in the summer here has jumped so much that crowding on the beach has become a safety issue for launching and landing the kites. One way to alleviate this issue was to provide compressed air to inflate the kites much more quickly then the regular hand pumps and get sailors off the beach quicker. This has been run by a gas compressor for the last two years and has proven a necessity for organization and safety.
Our air consumption changes drastically depending on user volume, day of the week, weather conditions, wind speeds (kite size) etc... So for simplicity the goal is to have this turbine operational with no CFM target in mind. Our storage tanks are 930L (2 x 420lb propane tanks) What ever the turbine can supplement to the gas compressor will be a great starting point.
Rotor diameter is somewhat capped at 6ft for the "social impact" at the site. Because of this I have been sizing a compressor to match the rotor. Settled on the Air-X Apollo blades off eBay so I could focus less on blade design and manufacturing and more on the mechanical structure.
http://www.ebay.ca/itm/6-x-62-Wind-Turbine-Generator-Blades-Hub-Nose-Cone-6-socket-fit-Air-X-Apollo-/361452233427?hash=item54283b62d3:m:m7XVhvn_Rp6sTpTfMh7q1OACut-In speed of 20kph in the goal for now.
Initial tests with these blades showed that coupled with a SV-202 (2hp rated) single stage compressor was too large for the wind speed range needed. This combo had a cut-in speed of 40kph.
I've now tested with a single cylinder .75hp compressor which works well but has some initial mechanical friction (piston rings) to overcome before the blades spool up. Cut-In speed was 50kph but was able sustain 50PSI down to 25kph once spooled up.
I've integrated automatic and passive furling with a spring and pneumatic cylinder.
Ok, now for the photos!
Main yaw bearing is a 1 1/8" bicycle head tube. Easy to work with, easy to find parts.

Large brass valve is a 3 in 1 check valve, compressor unloader valve, and adjustable pilot valve. The pilot valve supplies pressure to the 1/8" port once the tank has reached an adjustable set pressure, this feeds the extension port of the pneumatic cylinder and furls the turbine. The small needle valve keeps the tail from cracking the turbine in half when it furls at 160PSI! The pilot valve is vented to atmosphere when not engaged which allows the tail to return under spring tension.


This is the passive furling/tail return spring. Adjustments at both ends of the spring for tuning. A more permanent bracket will be made once a ball park spring rate and dimension is figured out in testing. Amazingly, my rough guess of rate and length furled the turbine at 70kph! This will change with compressor back pressure thou.


More photos in next post...