While I started this a few months back,
Work, no shop and other things keep me from finishing it.
When I tried to use a pop bottle shrink wrap the rotor didn't fit.

I got it back apart and with out the wrapper it fits very close
Of course I didn't repack the bearing and will have to do this all over again.

This was only a TEST fit and since I have it together-
I hooked up in 2y and 3 25Amp full wave bridges-
with two multimeters I can't get a reading
For a load I used a 1157 bulb and soldered bolth inputs to the pos wire
I read a while back about using a shoe lace to wrap around the shaft
and test pulling on it.
I used a 1/4" rope and this will get the bulb lit-up, No meter reading
I can just give it a 1/4 turn on the shaft with fingers and the bulb
lights up.
This only lights up about like the 28 Lb stepper motor I have,
maybe less.
When I take it back apart to re-pack the bearings, (I'll be using MARINE grade
Jet Pump grease), I'd like to get the shaft drilled and tapped for blade/hub
mounting.
That would require another trip to catch machine shop guy, and that can
be tuff sometimes.
Today I got offered a new better job that will have me working 5 AM to 2-3 PM. 
Because I have been getting to the shop at 7 AM and getting home 6-7-8-9 PM,
And they try to only want to pay for 8 but some times up to 13 hours and
at an amount lesser than told when starting and leaving a better paying job.
I TURNED IN MY 2 WEEK NOTICE This morning!!!!!!!!!!!!
~
New job also year round with bennies and 401K,!!!!!!!!!!!!!!!!
And paying better than crappy job I started for a friend in need.
Just two more weeks of heII and life should get better. 