3hp 3ph Baldor Permanent Magnet Conversion

After assembling this Permanent Magnet Conversion Generator we mounted it back in the lathe to do some testing of its output.

We purchased a 1200 volt, 140 amp, 3 phase Bridge Rectifier using Ebay for approximately $40.00USD + shipping. We did this so as not to have to build the rectifier bridge as another project. Not necessarily better just a shorter path.
We took a 12volt computer processor heat sink with fan and zip-tied it to the new bridge for cooling when testing. As a side note, if you look in the picture behind the bridge and heatsink you'll see a green dimpled cut piece of plastic. Just to share a great idea with you all, what that is is a two liter pop/soda bottle we used for shrink wrap when installing and uninstalling the magnet rotor in and out of the case while working on it to protect the mags from damage. The way you do this is just cut off the top and bottom and slide the remaining bottle body over the armature and use your heat gun or hair dryer and shrink the pop bottle down till it fits tightly over your armature... when you're done with its use just knick it with a knife and peel it off, it doesn't stick at all... pretty slick really and works great!

Next we zipped the bridge with heatsink to the lathe cross-slide table and then wired the generator. Fortunately when chucked up in the lathe fully assembled this generator fit very nicely to the ways with a piece of 2x2 as support and rotational stop. Kind of lucky really.

This is just a picture of the setup we used.
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(Note to self: Notice on Cut Red Wire, When using a 12 volt computer fan be sure to not exceed 12 volts. 183.1 volts certainly does make a 12 volt fan spin quite rapidly just before the smoke gets out.)
All the testing was done either open voltage or with 2-12 volt car batteries in series for 24 volts. The system this jenny will power is a 24 volt system.
Readings taken on lathe and with Schect rpm indicator to verify rpm
8-18-07
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Wired 1-Y no load AC readings
RPM
- 9.5 varying to 16.4
- 17v 35.3v
- 28v 42.6v
- 77v 84v
- 103v 106v
- 127v 140v
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Wired 1- Delta no load AC readings
RPM
- 9.7v 20v
- 17v 25v
- 16v 24.5v
- 44v 48v
- 59v 61v
- 74v 80v
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Next we wired a 140amp, 1200volt, 3-phase Bridge Rectifier
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Wired 1-Delta Open DC Volts
RPM
- 14.4 volt
- 19.2v
- 26.0v
- 61.9volt
- 81.2v
- 106.0v
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Wired 1-Y Open DC Volts
RPM
- 26.8v
- 35.5v
- 47.5v
- 107.0v
- 140.0v
- 183.1v
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Wired 1-Delta with 2 - 12 volt batts in series for 24 volts
Starting battery voltage was around 23 volts
317RPM 36.9volts at 8 amps
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Wire 2-Y with 2 - 12 volt batts in series for 24 volts
RPM
- 24.99volt at .44 amp
- 37.4 volt at 8 amps
From here on our lathe belt started slipping so we were
unable to accomplish better readings until we repair
the lathe but we did get a reading at:
RPM
370 38.8 volts at 9.33 amps
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The system that I have is a 24 volt system that has two battery banks. One is a set of 16 - C&D Liberty 1000's that are 100 Amp Hour SLA's, backed up by a Commercial 24 volt C&D battery charger system.

The other battery bank is a 48 Volt fork lift battery that has been split to be used as two 24 volt batteries in parallel. I also have another 36 volt fork lift battery that I'm either going to move to another location outside my system or split into one 24 volt that I could parallel into the existing 24 volt fork lift bank already mentioned and 1 - 12 volt arrangement. Interestingly all the batteries that I have, the fork lift and the Liberty's are manufactured by C&D Batteries as is the battery charger. The charger is temperature sensitive and does float, equalize and is totally adjustable.

It was also called to Kentt's and my attention that this jenny, due to soooooo many magnets on it, may try to make too much power so we thought that we would purchase something locally that could be used to control our magnetic flux with little effort. But what to buy? What could we get inexpensively that would get this jenny under control if it is developing too much flux? Well, we ran down to the local neo-magnet store here in the thriving metropolis of Yale, Michigan USA and bought the last, very last can of FLUX REMOVER SPRAY.
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Now comes the next learning curve. How to design a 3 bladed propeller that will match this jenny. We're using a furling mount of the Hugh / Dans design but a bit modified for our face mount jenny. We're located in Yale, Michigan with an average 5 -7 mph wind and have the advantage of a bit of a wind tunnel effect here due to the topography and woods locally. Our tower is at 65' and easily above any trees and more than 300' from the woodline.
We look forward to any thoughts, questions or critiques regarding this project and especially any thoughts on prop design.
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